A committee is a cul-de-sac down which ideas are lured and then quietly strangled - Sir Barnett Cocks

if a job 'aint worth doing well - outsource it and do it worse.

Read this, and then its antecedent here - and then wonder some more about TWA800 and 747 cargo doors that

 open mysteriously.

 

Difficulty Date : 10/11/00

Operator Type : Air Carrier

ATA Code : 5210

Part Name : CONTROLLERfrom the famous attorney, Gerry Spence, "I'm not going to guess whether there's a live bird or a dead bird in your hand; I'm telling you to open your hand!"

Aircraft Manufacturer : BOEING

Aircraft Group : 747

Aircraft Model : 747-422

Engine Manufacturer : PWA

Engine Group : 4056

Engine Model : PW4056

Part/Defect Location : CARGO DOOR

Part Condition : MALFUNCTIONED

Submitter Code : Carrier

Operator Desig. : UALA

Precautionary Procedure : NONE

Nature : OTHER

Stage of Flight : INSP/MAINT

District Office Region : Western/Pacific US office #29

A/C N Number : 199UA

Aircraft Serial No. : 28717

Discrepancy/Corrective Action: FWD CARGO DOOR OPENED BY ITSELF WHEN CB PUSHED IN. ON ARRIVAL, CIRCUIT BREAKERS WERE PUSHED IN, WHEN PRESSURE RELIEF DOOR HANDLE WAS OPENED THE DOOR LATCHES OPENED AND THEN THE DOOR OPENED ON ITS OWN. COULD NOT DUPLICATE PROBLEM AFTER INITIAL OPENING.

From AAR 92/02 United Airlines Flight 811

1.17.6 Uncommanded Cargo Door Opening--UAL B-747, JFK Airport

On June 13, 1991, UAL maintenance personnel were unable to electrically open the aft cargo door on a Boeing 747-222B, N152UA, at JFK Airport, Jamaica, New York. The airplane was one of two used exclusively on nonstop flights between Narita, Japan, and JFK. This particular airplane had accumulated 19,053 hours and 1,547 cycles at the time of the occurrence.

The airplane was being prepared for flight at the UAL maintenance hangar when an inspection of the circuit breaker panel revealed that the C-288 (aft cargo door) circuit breaker had popped. The circuit breaker, located in the electrical equipment bay just forward of the forward cargo compartment, was reset, and it popped again a few seconds later. A decision was made to defer further work until the airplane was repositioned at the gate for the flight. The airplane was then taxied to the gate, and work on the door resumed.

The aft cargo door was cranked open manually, the C-288 circuit breaker was reset, and it stayed in place. The door was then closed electrically and cycled a couple of times without incident. With the door closed, one of the two "cannon plug" (multiple pin) connectors was removed from the J-4 junction box located on the upper portion of the interior of the door. The wiring bundle from the junction box to the fuselage was then manipulated while readings were taken on the cannon plug pins using a volt/ohmmeter.  Fluctuations in electrical resistance were noted. When the plug was reattached to the J-4 junction box, the door began to open with no activation of the electrical door open switches. The C-288 circuit breaker was pulled, and the door operation ceased. When the circuit breaker was reset, the door continued to the full open position, and the lift actuator motor continued to run for several seconds until the circuit breaker was again pulled. At this time, a flexible conduit, which covered a portion of the wiring bundle, was slid along the bundle toward the J-4 junction box, revealing several wires with insulation breaches and damage.

UAL personnel notified the Safety Board of the occurrence, and the airplane was examined at JFK by representatives of the Safety Board, United Airlines, and Boeing. After the wires in the damaged area were electrically isolated, electrical operation of the door was normal when the door was unlocked. When the door was locked (master latch lock handle closed), activation of the door control switches had no effect on the door. This indicated that the S2 master latch lock switch was operating as expected (removing power from the door when it was locked). After the on-site examinations, the wiring bundle was cut from the airplane and taken to the Safety Board's materials laboratory for further examination.

The wiring bundle with the damaged wires contained all electric control wires (28 volt DC) and power wires (115 volt AC) that pass between the fuselage and the aft cargo door. From the forward side of the J-4 junction box, the bundle progresses in the forward direction, just above the forward pressure relief door, then upward, following the forward lift actuator arms. The bundle then enters an empty space between two floor beams, where the bundle has an approximate 180-degree bend when the door is closed. From this location, the wiring bundle progresses inboard, through a fore-to-aft intercostal between two floor beams. The wiring bundle then splits, with wires going in several directions.

The bundle is covered by the flexible conduit approximately from the lower end of the lift actuator arms to the fore-to-aft intercostal between the floor beams.

The conduit covering the wiring bundle is intended to prevent the wire bundle from being damaged during opening and closing of the door and during cargo-handling operations. The conduit is a sealed flexible inter-connector consisting of a convoluted helical brass inner-core covered by a bronze braid. The inner-core is soldered at every other convolute, and should be capable of withstanding pressures exceeding 1,000 pounds per square inch (psi). Boeing has indicated that the conduit is an evolutionary improvement and that it has been installed on all B-747 airplanes produced since 1981 (from line number 489 on). Airplane N152UA was delivered in April 1987.

Airplanes produced prior to 1981, including N4713U, used a bungee retraction system, to retract the cargo door wire bundle. Guidelines for the replacement of the bungee system with the flexible conduit were covered in Boeing Service Bulletin 747-752-2170, dated August 1981. The service bulletin was prompted by reports that the wire bundle bungee retraction system had not retracted the wire bundle sufficiently to prevent trapping the bundle between the cargo door and the door frame. UAL did not perform the retrofit on N4713U, which was line number 89, nor was the company required to do so.

Examination of the wires in the damaged area on the wiring bundle revealed that four of the wires were similar in appearance, with insulation breaches that progressed through to the underlying conductor. Adjacent to the breach on these four wires, the insulation was blackened, as if it had been burned. Another wire contained an extensive breach but no evidence of burned insulation. The damaged area was located on the bundle at a position approximately corresponding to a conduit support bracket and attached standoff pin on the upper arm of the forward lift actuator mechanism. This support bracket was found bent in the forward direction. In addition, mechanical damage was noted on adjacent components in this area.

A second damaged area was noted on the wiring bundle at a position approximately corresponding to the conduit swivel clamp at the elbow between the two arms of the forward lift actuator mechanism. Wires in this area were missing portions of their exterior coating, but no breaches to the underlying conductors were noted.

The exterior braid on the conduit contained minor rub marks and was slightly kinked at a position corresponding to the area on the wires with breached insulation. Additional examinations revealed that the inner-core of the conduit contained multiple circumferential cracks in the areas corresponding to the damage areas on the wires. The cracks were in the convoluted inner-core directly adjacent to the inside diameter of the conduit.

The lock sectors, latch cams, and latch pins from the aft cargo door were examined on the incident airplane and were generally in excellent condition. There was no evidence to suggest that the cams had ever been electrically (or manually) driven into or through the lock sectors.

Boeing also informed the Safety Board that, in May of 1991, a B-747 operated by Qantas was found to have chafing of the wires in the wire bundle to the aft cargo door. This airplane also had a flexible conduit protecting the wires, and the chafing was located approximately at the standoff pin on the bracket at the upper arm of the forward lift actuator.

The Safety Board determined that the chafing of the wires on the airplane involved in the JFK occurrence was caused by, or was greatly accelerated by, the circumferential cracks in the conduit and that the cracks in the conduit were caused either by repeated flexing of the conduit as the cargo door opens and shuts or by unusual stresses on the conduit generated concurrently with damage to the conduit guide bracket and attached standoff pin on the upper end of the forward lift actuator upper arm.

A portion of the wire bundle for the forward cargo door on many B-747 airplanes is also covered by a flexible conduit that is very similar to the conduit for the aft cargo door. However, there are substantial differences between the orientation of the flexible conduits for the two doors, and the Safety Board has not become aware of problems associated with the flexible conduit for the forward door.

Nevertheless, because of the concerns about the chafed wires and possible electrical short circuits, on August 28, 1991, the Safety Board recommended that the FAA:

Issue an Airworthiness Directive applicable to all Boeing 747 airplanes with a flexible conduit protecting the wiring bundle between the fuselage and aft cargo door to require an expedited inspection of:

(1) the wiring bundle in the area normally covered by the conduit for the presence of damaged insulation (using either an electrical test method or visual examination);

(2) the conduit support bracket and attached standoff pin on the upper arm of the forward lift actuator mechanism;

(3) the flexible conduit for the presence of cracking in the convoluted inner-core.

Wires with damaged insulation should be repaired before further service. Damage to the flexible conduit, conduit support bracket and standoff pin should result in an immediate replacement of the conduit as well as the damaged parts. The inspection should be repeated at an appropriate cyclic interval. (Class II, Priority Action) (A-91-83)

Evaluate the design, installation, and operation of the forward cargo door flexible conduits on Boeing 747 airplanes so equipped and issue, if warranted, an Airworthiness Directive for inspection and repair of the flexible conduit and underlying wiring bundle, similar to the provisions recommended in A-91-83. (Class II, Priority Action) (A-91-84)

The FAA responded to these safety recommendations on November 1, 1991, stating that it agreed with the intent of the recommendations and that the issuance of an NPRM was being considered to address the issues in the safety recommendations. The Safety Board replied on November 27, 1991, classifying each of the recommendations as "Open--Acceptable Response," pending the completion of the rulemaking process. Since that exchange of correspondence, the FAA has published an NPRM which is now being reviewed by the Safety Board. Safety Recommendations A-91-83 and -84 will continue to be classified as "Open--Acceptable Response" until an acceptable final rule is published.

 

The Stock Solution :  Wires with damaged insulation should be repaired before further service. 
When the going gets weird, the weird turn pro.

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