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Air 1997 |
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The Canadian Forces Directorate of Flight Safety (DFS) investigated
this occurrence on behalf of the Transportation Safety Board of Canada
(TSB) under the terms of the Memorandum of Understanding governing
Co-ordinated Investigations of Transportation Occurrences. This
occurrence was investigated for the purpose of advancing transportation
safety. It is not the function of the investigation to assign fault or
determine civil or criminal liability.
Aviation Occurrence Report
Loss of Control
Government of Canada
Department of Transport
Aircraft Services Directorate
Beechcraft King Air A90 C-FCGE
North Bay, Ontario
18 March 1997
Report Number A97O0043
Synopsis
C-FCGE, a Beechcraft King Air A90, was on a training flight in level
cruise at 11 500 feet above sea level (asl) in the vicinity of North
Bay, Ontario, when the crew experienced a vibration in their aircraft
and an uncommanded turn to the right. The decision was made to divert to
North Bay. During the descent, a
severe vibration developed and control of the aircraft was briefly lost.
After this severe vibration ceased and control was regained the aircraft
required significant left rudder to maintain co-ordinated flight. An
uneventful landing was completed. No injuries occurred.
Other Factual Information
The Beechcraft King Air owned by the Government of Canada and
operated by Transport Canada's Aircraft Services Directorate at Ottawa,
Ontario, was being flown by a crew of two on a routine training flight.
There were no other persons on board the aircraft. After an uneventful
first leg the crew landed in North Bay, Ontario at 1800 eastern standard
time (EST)(1), refuelled, carried out
normal pre-flight inspections and departed 45 minutes later for another
training flight with Ottawa as the planned destination after a
round-robin routing. After approximately one hour of flight, while in
level cruise at 11 500 feet asl, the crew experienced a slight vibration
and a shallow uncommanded right turn. The aircraft was returned to level
flight, the autopilot was selected off and a cockpit check was completed
when another uncommanded but steeper turn to the right developed. The
aircraft was once again returned to level flight and, as the vibration
was continuing, a decision was made to land in North Bay due to its
close proximity.
During
the descent, at approximately 8 500 feet asl, a severe vibration
developed which violently shook the aircraft and rapidly moved the
rudder and ailerons causing the hands and feet of the pilot flying to be
displaced from the control wheel and rudder pedals. After approximately
30 to 45 seconds, the vibration stopped and control was regained.
The descent was then continued at 140 knots, as the aircraft seemed
controllable at this speed. However, to maintain coordinated flight, the
crew had to hold approximately 2/3 left rudder. The remainder of the
descent, approach and landing were uneventful and the aircraft landed
safely. No injuries occurred. A maintenance recovery team was dispatched
and examined the aircraft. They determined that the hardware connecting
the rudder trim actuator push/pull rod to the rudder trim horn was
missing. After replacement of the missing hardware and a free play
check, the aircraft was ferried to Ottawa. The aircraft was returned to
service after a severe turbulence check and non-destructive testing
(NDT) of fittings in the empennage and wings.
The rudder trim is set by turning a wheel in the cockpit. This
movement is converted into a fore and aft motion of the push/pull rod.
The rod, attached by a clevis and bolt to a horn on the starboard side
of the rudder trim tab, displaces the tab either to the left or right.
This causes the rudder to be moved in the opposite direction thereby
trimming out the control forces necessary to maintain co-ordinated
flight. (See Figure 1)
The hardware attaching the push/pull actuating rod to the rudder trim
horn was last replaced when the aircraft was painted during the period
25 January 1995 to 10 March 1995. Since then, the last maintenance
completed in this area was the rudder trim tab free play check on
24 January 1997. Part of this check calls for a visual inspection of the
trim tab actuating system and directs that any inconsistencies be
rectified prior to the free play check. No problems were detected and
the component passed the check. As a result, the attaching hardware was
not disturbed during the process. The aircraft flew a total of 59 hours
between the free play check and the occurrence.
The Beechcraft 90, A90, and B90 Series Illustrated Parts Catalogue (IPC
Fig 54, page 3, Index #42) specifies that the attachment hardware used
to connect the rudder trim actuator include an AN173 bolt (no length
specified), two AN320-3 castellated nuts and two AN380-2-2 cotter pins.
The aircraft operator also uses Beechcraft 100 aircraft in a similar
role. The Beechcraft 90 and 100 are alike in many respects including the
rudder trim tab and actuator. The IPC for the Beechcraft 100 specifies
an AN173-5 bolt in this assembly along with one AN960-10L washer, one
AN320-3 castellated nut and one MS24665-132 cotter pin (IPC 27-21-01,
page 3, Index #3).
Inspection of other Beechcraft A90 aircraft used by the operator
revealed that the rudder trim actuator is typically attached to the horn
using an AN173-5 bolt, washers of varying thickness and number (to
ensure the correct orientation of the cotter pin hole in the bottom of
the bolt with the indentations in the nut), one AN320-3 castellated nut
and one cotter pin.
Analysis
Securing Hardware
The bolt and associated hardware securing the push/pull actuating arm
to the rudder trim tab horn was missing after the occurrence. There are
several possibilities as to why the bolt failed to remain secure.
Possibilities are - it was not there on take-off, it fell out at some
point, or it broke during flight. The first hypothesis is not likely, as
the crew would have noticed this during pre-flight inspections or in
flight prior to the occurrence.
In order for the bolt to fall out during flight the cotter pin would
have to either been missing prior to or broken during the flight, the
nut would have to back off and the bolt would have to move upwards
against gravity. The cotter pin was present during the previous free
play check and, as there is no force on the pin, it is unlikely that it
would subsequently break. Installations of this assembly were inspected
on the operator's other King Air aircraft and it was noted that the bolt
threads were painted. This would decrease the likelihood of the nut
backing off even if the cotter pin were missing. Furthermore, the bolt
is held in place by a bushing in the trim tab horn. The fit between the
bushing and the bolt is quite tight. This ensures that the rudder trim
will pass the free play check which demands a tolerance of only 0.021
inches.
The third hypothesis, that the bolt broke in flight, is the most
likely scenario. The fracture would not have been due to overload
stresses because there was no evidence of deformation on the clevis or
trim tab horn. However if there were cyclic loads of sufficient
magnitude present, the bolt could have failed in fatigue without
damaging the surrounding components.
As the shank of the AN173-5 bolt does not extend all the way through
the lower arm of the clevis, a fatigue crack could have developed at the
threads due to a stress concentration as a result of the shear load. The
shank of the bolt, however, is thicker than the threads and therefore
prevents them from coming in contact with the clevis and bearing any
load.
The bolt may have been manufactured from sub-standard material or not
been an aircraft quality part. As the bolt was not recovered, it was not
possible to examine it. Several samples of attaching hardware from the
parts bin in the operator's supply section (bolts, washers, castellated
nuts and cotter pins) were examined to confirm conformance with
respective specifications. Most met the specifications, however, one was
found to be non-conforming and many showed evidence of previous use
notwithstanding the operator's policy that only new parts are used when
assemblies like this are replaced. It is possible, that a sub-standard
part either similar in appearance to the correct part or purposely
manufactured to a lower standard and supplied as an aircraft quality
part, was mistakenly installed after the aircraft was painted by the
operator two years previously.
The bushing was recovered from the aircraft by pressing it out of the
horn. It was compared to another bushing from the operator's supply
section. The original was 0.002 inches in diameter smaller and had a
rougher finish than the new bushing. It was noted that it was difficult
to insert an AN173 diameter bolt into it. The normal practice when
completing this assembly is to try several bolts in the fitting and use
the one that gives the tightest fit. Given the close tolerances required
for this fitting and a bushing that had a slightly smaller inside
diameter, the possibility exists that a technician might have used a
non-conforming bolt in this installation if it resulted in the tightest
fit.
In summary the attaching hardware securing the rudder trim tab to the
actuator did not remain secure. The reasons for this could not be
conclusively determined.
Vibration and Loss of Control
The initial indication of difficulty during this occurrence was a
slight vibration and an uncommanded turn to the right. The vibration may
have been a result of a trim tab "buzz" due to play in the tab. The
amount of free play allowable in this mechanism is quite small (0.021
inches). As a result any wear on the bolt would have a
significant impact. If wear on the bolt progressed sufficiently to allow
vibrations or "buzz" to commence, the bolt could fail quickly.
Fatigue fractures of aircraft
bolts have been known to occur in cyclic load situations in a matter of
hours after installation(2). The
turn to the right could have resulted from a slight rudder trim tab
displacement as the bolt was wearing and the fitting was becoming
looser.
The second event that occurred was a severe vibration and loss of
control. Examination of the rudder trim system determined that when
disconnected, the push/pull actuating rod is free to rotate and/or move
slightly in the vertical or horizontal plane. If the push/pull actuating
rod moved slightly up or down the trim tab would be completely free to
move. As a result there is a possibility that tab
flutter could occur at airspeeds well below Vne.
If this occurred the result would be large
oscillatory displacement of the rudder.
According to the AGARD aerodynamics textbook "a number of accidents and
near accidents have occurred from flight failures in control linkages of
tab systems."(3) The large control
deflections and loss of control experienced by the flight crew could
have resulted from rudder tab flutter. The source of excitation, which
started the flutter condition, is unknown but a change in airspeed,
altitude and/or aircraft attitude probably was the cause of the severe
vibrations stopping. Fortunately, the flight conditions that initiated
the rudder tab flutter were not present for the remainder of the flight.
When the crew finally regained control of the aircraft they noted
that 2/3 rudder was required to maintain co-ordinated flight. If the
push/pull actuating rod moves slightly up or down and inward toward the
aircraft body, the arms of the clevis can end-butt against the horn (see
Figure 2) and force the tab to the left. If this occurred, the rudder
would be displaced to the right requiring left rudder input to maintain
co-ordinated flight. Tests on another King Air showed that when the rod
is in this position the trim tab would be displaced approximately half
its maximum deflection if the trim tab control started in the neutral
position. The air stream would be sufficient to hold the tab horn firmly
against the clevis unless another buzz was introduced. These tests also
showed that this was a fairly stable position for the clevis that would
not shift with control inputs or minor vibration.
Illustrated Parts Catalogue
The description of the attaching hardware for the rudder trim tab
actuator in the IPC for the King Air 90 is confusing when compared to
the IPC for the King Air 100. In the former the length of the bolt (IPC
Fig. 54, page 3, part 54-42) is not defined (i.e. should be AN173-5 or
-6) and, immediately following this entry, the IPC lists two castellated
nuts and two cotter pins which appear to be part of this assembly. The
extra nut and pin are actually used to secure the bolt (part 54-40) that
attaches the front of the actuator to the aircraft. As well, the
build-up description does not call for any washers, which are necessary
to ensure the hole for the cotter pin in the bolt is within the
indentations of the nut to allow the pin to seat properly. The IPC
for the King Air 100, on the other hand, lists these parts in a more
logical manner with each assembly (bolt and securing hardware) listed
separately. Beechcraft acknowledged this
inconsistency and is amending the IPC to correct this deficiency.
Standard industry practices, as used by the aircraft operator's
technicians, would call for the use of washers in the attachment for the
King Air 90.
The Canadian Air Regulations (CAR) prohibit the substitution of parts
listed in the manufacturers IPC unless accompanied by approved data
acceptable to the Minister(4). A
technician referring to the IPC for guidance on how to attach the rudder
trim tab actuating arm to the horn would be faced with an obvious error
in the parts list. According to the CARs, an operator faced with this
dilemma must identify the problem to the manufacturer and then wait for
him to amend the IPC or issue data acceptable to the Minister to
substitute the specified parts for a more logical assembly. This delay
could result in an unacceptable grounding of an otherwise serviceable
aircraft. Previously an operator could refer to a substitution guide or
similar document and install an equivalent part identified therein in
cases such as this. With the onset of the CARs, this is no longer
possible.
Before the enactment of the CARs the operator handled this
discrepancy by either referring to the IPC description in the King Air
100 manual for guidance on how to complete this assembly or using the
identical build-up that had previously been installed.
Findings
- The attaching hardware securing the rudder trim tab to the
actuator did not remain secure. The reasons for this could not be
conclusively determined.
- Tests of a sampling of attaching hardware from the operator's
supply system revealed one bolt which did not conform to the AN173
specifications and several that showed evidence of prior usage.
- A minor vibration and uncommanded right turn developed, which the
crew was able to control.
Later a severe vibration developed, which resulted in the crew losing
control of the aircraft, but the vibration stopped when the parameters
that sustained it changed as the aircraft descended. Left
rudder was then required to maintain co-ordinated flight.
- The King Air 90 IPC does not identify the
length of the bolt to use to connect the actuator to the horn.
As well, the description of the assembly is
confusing and not consistent with how the King Air 100 IPC describes
the assembly. The assembly normally used was an AN173-5 bolt,
two washers, an AN320-3 castellated nut and a cotter pin.
- The Canadian Aviation Regulations do not permit the substitution
of parts listed in the manufacturer's IPC unless accompanied by
approved data acceptable to the Minister of Transport.
Causes and Contributing Factors
The bolt securing the rudder trim actuator to the rudder trim tab
horn became detached for reasons that could not be conclusively
determined. The rudder trim tab was then free to either oscillate or be
held to the left by the disconnected trim tab actuating arm.
Lack of detail and an inconsistent and confusing description of the
parts required for the attachment of the actuating arm to the trim tab
in the Illustrated Parts Catalogue as well as the possibility that a
non-conforming bolt was used when the fitting was last installed may
have also contributed to the bolt not remaining secure.
Safety Action
Action Taken
Immediately after the occurrence, the operator inspected the rest of
their fleet to ensure the condition and conformity of the Rudder Trim
Tab attachment hardware.
Action Required
TSB liaise with Transport Canada to have Beechcraft review and revise
the IPCs of the Beechcraft 90, A90 and B90 aircraft to reflect the
correct AN hardware for the rudder trim tab to rudder trim actuator
attachment.
TSB liaise with Transport Canada to have CAR 571.13 revised to make
it more realistic and operationally feasible for operators.
Initiatives currently underway throughout the aviation community to
identify and eradicate non-conforming parts be continued. While this
occurrence cannot be positively identified as being due to this problem,
it is a possible scenario that cannot be eliminated. Education of
aviation personnel, through this and similar occurrences where problems
associated with these parts are revealed, should continue.
Department of Transport - Aircraft Services Directorate institute
procedures to ensure that all parts issued from their supply section
conform to the specifications required in appropriate publications.
ADDENDUM
The following actions have been taken by the TSB and Transport Canada
in addressing the Safety Actions Required, as in the public report:
- Transport Canada has written the Federal
Aviation Administration recommending that Raytheon Beech be contacted
to have the Aircraft Maintenance Manual amended to include complete
assembly instructions and illustration.
- Transport Canada does not recognize the Illustrated Parts
Catalogue as an authoritative document for the purposes of assembly,
only for the identification of appropriate parts. Therefore, Transport
Canada does not agree that CAR 571.13 should be revised.
- Transport Canada, Aircraft Services Directorate, has verified that
all parts in their parts supply section conform to the required
specifications and are in the appropriate bins. This activity is
on-going.
All warehouse and procurement staff and aircraft maintenance
engineers (AME) in the Aircraft Services Directorate have received
training on bogus parts to increase awareness on this issue.
The Aircraft Services Directorate Maintenance Control Manual was
amended to enhance parts control procedures.
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