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Quote: At about 700 ft AGL, the auto throttle commanded
engine acceleration. One engine started to rollback during
and the other engine started to accelerate then 8-10 seconds
later began to roll back. Once the flight crew noticed, they
pushed the throttles up and the engines' EECs responded but
the engines did not. It appears that no fuel was getting to
the engines.
The investigation continues to look broadly for a cause of
the dual engine rollbacks. Fuel exhaustion is the only item
that has been positively ruled out. Aspects that the FAA
believes the investigation is concentrating on are:
• Ice in the fuel somehow limiting the fuel flow to the
engines. A maintenance message
indicating excessive water in the center tank was set during
taxi on the two previous flight legs, although it cleared
itself both times. The airplane was being operated in a high
humidity, cold environment, conducive to ice formation.
• Small-sized contamination building up in the engine fuel
systems somehow limited the fuel flow to engine. All the
fuel samples have tested for contamination of larger
particles (sizes outside the fuel specification). Testing
has been started looking for small particles (greater than 5
microns).
• Engine hardware failures sending inaccurate data to the
engine electronic control (EEC) causing the EEC to demand
insufficient fuel. A preliminary review of the EEC data from
the right engine shows erratic combustor inlet pressure
(P30). A leaking P30 sense line could cause this, or the EEC
receiving a higher than actual fuel flow parameter.
• Software coding problem in the EEC
causing the EEC to demand insufficient fuel. British Airways
installed a new engine EEC software revision in December
2007. The software was approved in May 2006. There were
several changes to the software as part of the revision. Two
items seem remotely related to the accident: improvements to
low power stall recovery logic and fan keep out zones for
ground maintenance. The first two items would be
related to a part 25 compliance issue, while the last two
items would be related to a part 33 compliance issue.
As stated yesterday in this briefing paper, the electrical
system anomalies noted earlier have been resolved, as
describe below, and the conclusion now is that the
electrical buses were powered until impact and performing as
expected.
• The auxiliary power unit (APU) began its auto start
sequence, even though the buses were still powered. In the
days following the event, the flight crew has added
additional details to their report. The crew now believes
they turned the APU on prior to impact. There was sufficient
time before the impact for the APU inlet door to open, but
not for the APU fuel pump to turn on or the APU engine to
start spooling up.
• The quick access recorder (QAR) saved data and shut down
approximately 45 seconds prior to impact. The QAR saves data
in batches. It is believed the QAR was working properly and
unfortunately, was still in the process of saving data when
impact occurred, accounting for the “lost” 45 seconds of
data.
• The fuel crossfeed valves were closed in flight according
to the flight crew, but the switches were found in the open
position and only one valve was open. In the days following
the event, the flight crew has added additional details to
their report. The crew now believes they opened the valves
just prior to impact and the airplane lost power before both
valves moved to the open position.
• The ram air turbine (RAT) was found deployed, even though
the buses were still powered. It did not deploy until after
the airplane came to a stop, as determined by the pristine
condition of the turbine blades. The RAT either deployed due
to electrical power loss during impact with a failed
air/ground signal or the impact unlatched the RAT door.
Fuel system: Leads regarding water in the fuel and
fuel contamination are continuing to be investigated. Fuel
testing looking for small-sized contaminants (5 microns) is
beginning. The tanks are still being drained and the team
hopes to start evaluating the fuel system hardware tomorrow.
Engines: Component testing and teardown of the
engine-driven fuel pumps and the fuel metering units is
planned for later this week. The data from the electronic
engine controls is still being analyzed. Rolls-Royce is
planning an engine test, unscheduled as yet, to try and
duplicate the rollbacks.
Crashworthiness: Cabin crew and passenger
questionnaires indicate that the evacuation bell was faint,
but the evacuation light was seen and the captain’s message
to evacuate over the passenger address system was heard.
Preliminary data indicates that the descent rate at impact
was roughly 30 ft/sec. Dynamic seat requirements that became
effective at the introduction of the Model 777 series
airplanes require that seats should protect occupants for a
hard landing impact of up to 35 ft/sec. The passenger with
the broken leg was sitting next to the point where the right
main landing gear punctured the fuselage and pushed into the
cabin (pictured below).


Crashworthiness: There was only one serious
injury, a compound fracture to the leg. The airplane landed
on the main gear, bounced, came back down on the gear, then
the gear failed, and the engines supported the weight of the
airplane. The descent rate at landing was 1500-1800 feet per
minute. One of the main landing gear bogies swung around and
pushed slightly into the cabin (see photos above). The other
punctured the center fuel tank (empty) leaving a 1-by-2-foot
hole. The report of a fuel leak is unconfirmed. All the
slides deployed and the doors worked. Some passengers had to
shuffle down the slides due to the slight angle. The flight
deck door opened on its own during the landing. Some oxygen
masks dropped. from
this link |
Now....... Does "crossfeeds 1 out of 2 open" show the
Captain had done the drill as quick as he could after
failure?
...OR, selected a little earlier as a precaution, whereupon
ice or wax sludge got to both engines?
...OR, were they both selected open for some considerable
time for some reason , but one crossfeed valve failed
shut (due to an ice/wax slug)?
We know that OATs were excessively low for quite a long
time...I'd like to know the history of the fuel temp time
line throughout the flight and any action taken, and the
last logged fuel quantity and planned reserves
...Impact Rate of Descent 1800fpm or more and a helluva
flare needed..and thus has to be perfect.
... Looking at the flight path not far off 600 or 700 fpm it
may have actually stalled 2/3rds of a second, 120 feet,
before touchdown |